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we have seen errors where the BMI088 gets out of sync, so that the 3 axes are rotated. The data is shifted by 4 bytes, so that X=Z, Y=X and Z=Y this changes the BMI088 to "stop on full" mode, which is what Bosch use in their example drivers, and also catches FIFO overrun events and triggers a full FIFO reset. This should fix the problem with the FIFO syncCopter-4.2
Andrew Tridgell
3 years ago
committed by
Randy Mackay
1 changed files with 20 additions and 17 deletions
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